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For this pollution prevention effort, the plant's objective was to locate all the uses of Freons and Halons and replace it with substitutions or totally eliminate the process. The program began in the mid-nineties to remove the Freon-11 chillers and replace them with units containing HFC-134a. In 2000, a $1.2 million project was initiated to remove all Halon 1301 from the spray booth fire protection systems, the computer room and the Electrocoat Laboratory and replace them with a non-ozone depleting substance FM-200. In total 1.3 tonnes of CFC and 3.3 tonnes of Halons were removed from the plant. As a result, 4.6 tonnes of ODS products were eliminated from the plant as well as the risk of inadvertent emissions through upsets or accidental releases that may be harmful to the ozone layer. Paint Use Reduction Ford Motor Company of Canada, Limited Oakville Assembly Plant (8th Progress Report) The Ford Oakville Assembly Plant manufactures the Windstar minivan for the global market. The plant is located on a 487 acre site on the same property as the headquarters of Ford of Canada and the Ontario Truck Plant. The facility has a 3.8 million square foot floor area and employs approximately 3,200 people. Production first began in 1953. Under the Performance Standard Guideline set out by the Canadian Council of Ministers of the Environment (CCME) (August 1995), it was recommended that the coating facilities of original equipment manufacturers (OEM) limit their volatile organic compound (VOC) emissions to 60 g/m2 by the year 2005. With the implementation of several VOC reduction projects, the Oakville Assembly Plant has achieved a 30 g/m2 VOC actual cumulative average in 2001, which means its VOC emissions are 50% below the CCME target.
Reducing paint use and limiting the paint process to one reciprocator zone decreased the need for paint and cleaning solvent. This project therefore reduced VOC emissions by reducing usage of solvent and paint overspray that occurred in the second reciprocator zone. The objective of the pollution prevention effort was to reduce usage of paint and solvent, which contain VOCs such as methyl isobutyl ketone (MIBK), xylene, n-butyl acetate, and 1,2,4-trimethylbenzene through process change. The result was that there was a reduction in paint and solvent usage of 77 tonnes per year, a 20% VOC emission reduction. Improved Paint Transfer Efficiency Using Rotary Bell Applicator General Motors of Canada Limited Oshawa Truck Assembly Plant (8th Progress Report) The General Motor's Truck Assembly Centre in Oshawa builds Chevrolet and GMC Pickups -1/2 ton capacity models in two and four wheel drive, shortbox and stepside extended cab versions. The Truck Assembly Centre is on the site of the GMCL Oshawa Autoplex, which is the largest North American Automotive facility, occupying over 110 hectares of floor area. Utilizing 30 hectares of the floor space, with state of the art assembly facilities and synchronous manufacturing techniques, the Truck Plant produces approximately 1300 vehicles per day. Other operations on the Autoplex site include Car Assembly, Stamping operations, Tri-Link fabrication, and Battery manufacturing. Oshawa operations employ over 12,000 people.
The Oshawa Truck Assembly Plant, in cooperation with Sames, Fanuc and General Motors North America paint group, developed a rotary bell applicator - "Aquabell" - for waterborne electrostatic paint application. The rotary bell applicator can improve transfer efficiency by more than 20%. The Oshawa Truck Assembly Plant is the first assembly plant to implement the Aquabell applicators within General Motors. All of the robots that apply basecoat at the Oshawa Truck Assembly Plant are being converted throughout 2001 and 2002. This process redesign pollution prevention initiative was intended to address all media land, water and air by improving paint transfer efficiency. By improving paint transfer efficiency the assembly plant realizes several business, operating and environmental benefits concurrently paint usage is reduced, paint cost is reduced, air emissions are reduced, waste paint is reduced and less cleaning needs to be done in the spraybooths. Volatile organic compounds and semi-volatile organic compounds that are used in the basecoats: n-butyl alcohol, methyl ethyl ketone, xylenes, 2-butoxyethanol, 1-methyl-2-pyrrolidinone, ethylene glycol were targeted for reduction with a 20% improvement in transfer efficiency with the associated improvements in paint usage, emissions and waste generation. As a result, the efficiency was increased by more than 20%. This means less paint needs to be sprayed to achieve the same quality and appearance characteristics. In addition, paint savings are more than 300,000 litres or $5 million per year were realized. With the reduced paint usage Volatile Organic Compound (VOC) emissions have been reduced by 60 tonnes annually. Furthermore, waste paint has been reduced by 88 tonnes which translates to 30 tonnes less paint sludge going to landfill. Available Publications and Information on Pollution Prevention
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